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    Results 141 to 152 of 152
    1. #141
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      In the latest news, I've been out of the garage for a couple of weeks but I'm slowly getting back to it. I drove the car again a short distance and made note of the things that I wanted to address. First off, I wanted to add a catch can to the radiator. The main reason for this is because I have a shop cat and I don't want the car to burp or drool one day and the cat to find the green puddle interesting. It's more for peace of mind for me and safety for the fuzzy knucklehead. Second thing I wanted to address is the power steering pump. It was a little noisy after my short drive and I wanted to get ahead of any issues that may arise. I know the steering box is getting hot because the header is incredibly close. I opted to put a heat shield over the box as well as lower the pressure and flow from the pump since I found that the Borgeson box prefers both lower than what the pump is supplying. I will also be adding a ps cooler.


      Not all of my parts have arrived yet. I'm waiting on the pressure and flow valves to arrive today. I'll likely knock that out by the weekend and post updates then.


      The catch can is from Summit. I wanted something better than the tiny inlet on it so I cut off the existing one and tapped it for a 1/8npt elbow. After that was done, I mounted it to the passenger's side of the radiation near the cap.











      Here is the shielding material I got from DEI. It is good to 1400 degrees so should be fine for what I'm doing. I roughly attached it to the steering box with stainless zip ties.








      Kris - Building the poor man's '68 Mustang.

    2. #142
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      Last weekend I decided to replace the fitting and shim the flow valve in the PS pump. This will bring the output of the pump to the levels of pressure and flow that the Borgeson box prefers. The pump specs list 1400 psi @ 2.5 - 3 GPM and the box lists optimal specs at 1100-1250 psi and 1450 max @ 2 - 2.5 GPM. I may be overthinking all of this but that's what I do.
      I pulled the fitting that came with the pump out and used the shim kit from borgeson to lower the pump pressure. I then reassembled the valve and replaced the fitting with a lower flow one that has a male -6 output. I didn't like having a fitting adapter in line that could introduce one more leak point, so the one-piece fitting was chosen. After all of that was done, I reinstalled the pump. Now I just have to reinstall my lines, mount and plumb the cooler and fill and bleed the system. In theory!

      Borgeson's pressure kit includes the clamp for the pressure valve to prevent damage to the valve while holding it steady in a vice. It also has the shims needed to raise/lower the pressure. Just follow the instructions to choose the appropriate number of shims under the screened bolt to reach your target pressure.





      This weekend I finished adding my power steering cooler and hooking all the lines back up and everything seems to be all good again. A buddy (66 coyote-swapped mustang) kept pushing me to go out and get some shakedown miles with him so Sunday was shakedown day.
      He drive about 30 miles to my place and then we drove out to a nearby lake to put a few miles on my junk. Neither of us thought about how crazy the traffic would be. It was still a nice drive and neither car had any issues. We poked around on the crowded twisty roads before heading back to my house to give both cars the once-over. Progress!





      Kris - Building the poor man's '68 Mustang.

    3. #143
      Join Date
      Dec 2006
      Location
      SF Bay Area
      Posts
      456
      Nicely done. Progress is progress.
      chunger

      '68 Ranchero 500
      '70 Cougar XR-7 Convertible
      '98 Mustang GT Convertible

    4. #144
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      It's been a minute!

      Let's see. A quick recap of the past 6 months: For the sake of making this easier, I'll copy/paste from my build thread from the VMF.

      April 2023:
      I messed with the alignment a bit. Ordered turn plates and a hub adapter to help dial everything in. Got confirmation this morning that my Dyno-day will be May 1st at 9am. I guess I need to get about 400 more shakedown miles on this pile before then!

      I was out at AMP saturday to watch the SCCA guys fling cars around. I left my place early-ish and stopped by to wake up a buddy and we drove out. No real issues to speak of with the trip. I was able to get out there and back and add around 100+ miles to the clock. I spent Sunday messing with the alignment more and ordering parts to start sealing up my interior and prep for dyno day.



      Pre-Saturday drive: I checked the Tefba filter and found some junk in it. Looks like edges of gaskets that were in the flow path and got softened up and broke free. I've seen no coolant leaks aside from a tiny bit of seeping around the thermostat housing. I'll keep an eye on it.





      Saturday on the way home, the I-10 and 202 split was a mess. I stopped off at work to refill my water bottle and stretch my legs for a minute.



      Sunday, I got to work trying to dial in the alignment. I'm using a digital Intercomp caster/camber gauge that a friend brought over. I picked up one of their hub adapters to mount it directly to my spindle.
      Test fit. I took all of the measurements with the cotter pin and nut retainer off.



      I'll end up having to shim the UCA to get caster where I want it. I was only able to get +2* caster before i ran out of room with the front of the tire and the fender on turns. I have shims ordered and they should get here Tuesday.





      I buckled to peer pressure. I blame my friend, Dan.

      This was a dyno day at a friend of a friend's place on sunday. Aside from our two classics, there were 5 foxbody ltd wagons, and the homeowner's 800 hp lx coupe, his early bronco, his wife's yellow gt seen behind mine, etc, etc. The guy in the vid on the right has one of the wagons. It's green with qcumber on the tag and powered by a turbo'd 5.0. There was quite a showing of people. The neighbors probably loved it.

      With no tuning at all, and the EFI still in learning mode: 375hp @ 5400 and 410 ft lb @ 4200. It'll be fun to see what next week's tuning session will bring.

      https://youtu.be/_rO49RyDi_Q

      May 2023:

      Bleh. Tune day was yesterday. I spent the weekend going over a few things and whatnot. I changed the oil and plugs. While changing the oil, I found that my pan gasket is drooling. Decided to put that on the list to replace. In the process of changing the plugs, I managed to rip the plug boot on the number 2 cylinder. I had to rummage around in Autozone trying to find a single wire that would work well enough to get to the tuner and make it through the day. Got that sorted out and chose to try to find something that would be a bit more relaxing, so I decided to install my shift boot and bezel. I also started to line the inside of the firewall with 1/2" Dynaliner as well as plug the unused holes.
      Got ready to crank the car after the oil and plug change and noticed my courtesy lights weren't on. In trying to figure that out, I found blown fuses for the hazards/stop/courtesy lights. Great. I pulled the steering wheel to make sure there wasn't anything going on with the signal switch. I found that the horn contact rings on my pricey grant hub weren't centered correctly and one had started to peel off. More great news. Problem to address later. In the end, I found that my third brake light wire had been pinched in the trunk and was causing the short. Easy fix.

      I get to the tuner on time, drop off the car and head home. The slot was from 9 to 1. I get a call a bit after 12 with 'good news or bad news first?'........
      Good News: The tune is completed. The engine is dialed in and healthy but I was a little disappointed with the final numbers. After running hard all day getting tuned: 365hp @ 5200 and 406lbft @ 4000.
      Bad News: the engine spit out another freeze plug on the last pull......That's 2nd of 6 to let go. I called the builder, raising the question to him as to 'why?' and maybe a little bit of hell during the call.

      The long and short. The car is home. Sitting ignored in the garage until I feel like pulling the engine. I don't trust the other plugs, so I will replace them all. I'll replace the pan gasket while it's out.

      At least this looks nice.


      This was more than a bit irritating to find.


      Not at all pleased about this. The dirty spot on the boot is from my grubby finger admiring the split. The missing boot was used on the temp replacement wire from autozone. I have replacement ends arriving today. I'm sure I'll get right on that.....


      There isn't enough profanity to describe my displeasure.


      And here's an expensive piece of paper with a visual representation of my efforts.
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      Technically, it's close to what the builder estimated when we were going over the build. He was estimating 425ish hp and 450ish lbft torque at the flywheel. That would roughly equate to the numbers I got if you subscribe to the 15% loss from flywheel to rear wheels theorycrafting.

      I've decided to go ahead and pull the engine and replace them all. I don't want it to strand me. I'll also do a combustion gas test when it's all back together for added piece of mind. And it's still a riot to drive when you stomp on the gas, so I'll be ok with my numbers....for now!
      Kris - Building the poor man's '68 Mustang.

    5. #145
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      May 2023:

      Yesterday, the 66 coyote friend offered me his truck, hoist and engine stand. He only lives about 10 minutes from the office, so I had my boss drop me off in the work car and I picked everything up and headed back to work. I convinced my boss that it was an incredibly slow friday and that I'd be happy to drop him off on my way home (it wasn't hard to do since his grandkids where in town) He agreed and we got out of work at 1. I got home and started prepping to pull the engine.

      Saturday morning! Took my time getting everything ready. Stopped for lunch and then got back to it. The engine is out and ready to go on the stand. I had to run out and pick up a socket for the flywheel bolts. Apparently, I no longer have the 1/2 drive 3/4 12 point socket that I thought I did. Anyway, I'm starting a list of things I'd like to address while the engine is (back) out. Wiring cleanup, shock tower reinforcements, extra heat control under the floor, and some plug boot protectors. Anyway, progress! I'm trying to stay positive about having to pull out the engine.

      This happened while on the dyno. I'll be investing in boot protectors.



      I went back and forth about the pricey Mac's pivot plate. I ended up getting one and I'm pleased with it. It made getting the engine out easier. We'll have to see how well it does going back in.





      I plan on reinforcing the shock towers. I'm not sure how much of a gap is normal, but I'll adjust mine with a hammer to close them up before welding.

      Passenger side:







      Driver side:








      I'm going to rename this project: "While I'm here...."

      I was working on replacing the freeze plugs and cleaning up old oil pan gasket material from the block surface this Sunday. As I was scraping gasket off, I thought I caught a glimpse of a piece of gasket fall into the timing cover. Great. Get the flashlight and look around, don't see anything. Look around on the floor under the engine, don't see anything. Look in the block, don't see anything. Get my inspection camera and laptop out, don't see anything. I stop for lunch and it kept nagging at me. So I place an order for a timing cover set and pull the cover. No gasket piece behind the cover....oh well, I've got timing cover and water pump gaskets on the way. I also remembered that I wanted to replace the thermostat gasket. That stuff will arrive Tuesday. Once it all gets here, I'll try to finish buttoning up the engine. I still haven't reinforced the shock towers or done anything in the engine bay yet. I'll get there.



      Spent a bit of time over the weekend making progress. The engine is buttoned back up. I'm waiting on the AC kit to arrive so I can get started on that.

      Deep freeze plugs and Ford Motorsports oil pan rails were added.



      Engine flipped back over and ready to go back in when the time comes. I'm gonna be so disappointed if this thing leaks again. (foreshadowing)



      The latest news. Not a whole lot going on, really. I called Desert Classic Parts to pick up the factory-style ac vents for my vintage air setup that I have coming. Bill was super helpful and accommodating. I opted for the factory-style vents because I really prefer the look over the 'below the dash' vents that come with the VA kit. I got a killer deal on the vents and they look fantastic.



      I also called Vintage Air this morning to switch out the controls to make sure that everything works well together when the kit arrives. The change will delay my order for a few days, but it'll be worth it.

      I finally stitched-welded the shock towers because I figured it was the best time to do it since the engine was out of the way. I scuffed everything up, zipped it together, and then squirted some black paint on it.





      Aside from that, I've picked up longer hoses for my lift. I got tired of tripping over the hoses and will be mounting the controls on the wall next so it's not on the floor and then running the hoses overhead so they're out of the way. I'll probably work on that this coming weekend unless my ac kit shows up earlier than expected. Maybe Dan will stop by to hang out if he's not wasting his weekend playing golf!

      Oh, and I put new tires on my daily.....because I'm a responsible adult.

      June 2023:

      Still waiting on the AC kit to arrive. I did finally get around to wall-mounting the lift controls. I went overboard but I'd rather overdo it than have it fall and break something. Everything is back to working order. I will need to re-grease the lift blocks to address the jumpiness of the lift when it's on the up-travel. I'll get to that this weekend. I tested it by lifting the car and promptly used that opportunity to apply some heat shielding to the floor above the area that the headers are. Back to waiting on parts.....







      Made progress on getting AC all mounted up in the car. Hanging upside down in the floorboard while holding up an evaporator is so much fun!
      I believe that I'm ready to stab the engine back in now. Once that's done, I'll start sorting out lines for the AC.

      I will have to reroute and clean up a lot of my wiring since I no longer have a big empty space under the dash to leave it all.



      Kris - Building the poor man's '68 Mustang.

    6. #146
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      July 2023:

      I'm on vacation!
      Made a run up to Las Vegas for a couple of days to reconfirm that I am not that city's target audience. Living in New Orleans for my younger years filled my social meter for a lifetime.
      I did get the engine back in the car before leaving!



      While in Vegas, we stopped by the Shelby American shop to poke around.







      But, we're back home and all is well. I've got parts over at a friend's that will get dropped off at work when he's free. I also ordered a replacement fresh air vent since mine was trashed and had a hole in it (from the bullet that went through the A pillar and under the dash). It is currently sitting in the garage completely disassembled and soaking in evaporust since it looked to have been holding lots of dirt and leaves in it for quite some time. I'll get back to work this weekend putting everything under the dash back together so I can start getting this pile back on the road.


      Made some progress today. I didn't get pics of it, but I put in a retrosound 5x7 in the dash. I also added some speaker grill material over the actual speaker to try and help cut down on the dust (because everything is dusty in the desert) that collected in the speaker.
      I also started running ductwork for the ac.....it's a snake's nest under there. To make it worse, I also added the fresh air vent back in on the driver's side. Tomorrow will be spent running the wiring for the AC and cleaning up the existing wiring since I moved everything out of the way to make the duct work easier. I also ordered a headliner from MTF. It's sitting over at Dan's place. I will work on getting that installed sooner or later.







      Spent some time in my garage this weekend. I was putting my portable AC through its paces. I had a goal of getting the duct work and wiring sorted out and the dash completely assembled.
      By 4 on saturday, I had everything routed under the dash before calling it a day. Sunday, I had to reroute some of the ducts to prevent them from rubbing against the wiper mechanism (not an easy task) and finish running the main power wires. I was able to get most of that all wrapped up and now my dash is more complete than it has been since January 2020!

      Kris - Building the poor man's '68 Mustang.

    7. #147
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      August 2023:

      I've made progress on the ac. I have the dash completely reassembled for the first time in many years. I'll have to be creative for the radio bezel because the ac ducts take up the majority of the space behind the dash. I've considered finding a non-working factory AM radio and taking it apart and just using the face to fill the space. I'll sort that out later. Dan dropped off my Mustangs to Fear ABS headliner and I got that installed. It's in place right now and I'm leaving it alone for a few days to let it 'settle' before doing a final fitting. I also got the heater hoses and routing done. I had to chase down a fitting at a local shop because the one I had is buried in one of my boxes. I'll find it later. I also reinstalled the windshield and back glass trim.
      I've been working on the interior stuff because I'm waiting on some hard lines from Vintage Air to arrive. I bent some templates up to run from the condenser into the engine bay. I figured that would be cleaner than trying to do rubber hoses. Once those arrive (2 weeks-ish?) I'll get back to wrapping up the AC install and getting the car back on the road!

      As you can see, there's little to no room for the massive factory head unit. That's why I had considered making a facade with a broken factory AM setup to clean up the look.



      Heater hose routing. Since my engine sits down, back, and to the passenger side, I opted to use a preformed hose (Gates 18774) to help clear the block. It worked out well enough, I think. The first pic is the fitting I had to chase down because the one I had is sitting somewhere in a box laughing at me.





      Windshield trim and wipers back on!



      Mustangs to fear headliner in. Yes, those are footprints. I was in the car and on my back installing it solo since I am stubborn and didn't want to pester the missus to assist. The fit at the a pillar covers isn't ideal but that's why I was going to leave everything in place to let it settle before I started to trim anything or drill holes.







      My hard lines from Vintage Air arrived yesterday. They turned out great. I spent this morning mocking up my soft lines and getting all of that ready. I'll take them to work and @Anangryford knows a guy that will crimp them for me. Once I get those back, I'll be ready to button this pile up and get it back on the road.

      When I made the line templates, I wanted to be sure that the lines cleared the fasteners for the radiator and went through an existing core support hole. I was pleased with the fit. The only thing I had to do was move the condenser over just a bit to give me room between the lines and the edge of the hole in the core support. That was as simple as loosening the screws and sliding it over since the mounting holes are slotted.











      I also took the old radio apart that I picked up on ebay and got it mounted in the dash. I'll still need to move some ductwork around because it's still pushing a duct up high enough to hit the wiper arm. I'll get some pics of the radio as it sits now when I'm back outside.
      This is where I started. My original working one is on the left.



      Radio pics after removing the majority of the body. I wanted to retain the buttons and knobs as well as the light. The tuning knob and station buttons still work but the power/volume button was sketchy at best when I took it apart and just free spins. No big deal. Everything is back in the car now and I'm looking forward to getting the AC lines crimped and getting this pile put back on the road!



      Kris - Building the poor man's '68 Mustang.

    8. #148
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      September 2023:

      I've been on a self-imposed break from the car. Several posts back I stated that I would be very disappointed if this thing leaked. Well, it leaked and I addressed the leaks. And then things I haven't touched before that -weren't- leaking, leaked..... Anyway, still haven't drawn down the ac system or charged it yet. I've been fighting with a drooling cooling system. I will say that the Gates Powergrip shrink clamps are great, if you don't have to keep taking stuff apart.

      Anyway, the ac lines are crimped and in place. I filled everything and pressure tested the car only to find a drooling water pump. Apparently, I had failed to properly seal the pump against the timing cover. I commence to tear everything back down, replace the pump gaskets and reseal them, reassemble everything, fill it, and pressure test again.....and the lower radiator hose starts peeing. So many profanities in such a short amount of time. I went ahead and started the car so I could do a combustion gas test. After the second core plug popped out, I wanted to be sure that I wasn't having those issues because of a head gasket or block leak. That test came out fine.

      So I order another lower hose and wait for it to arrive. It shows up and is just different enough that it doesn't fit (the downside of using non bolt-in stuff). So I proceed to cut/trim it to fit. I place an order for the stuff I'll need to button that up and give the car the middle finger and walk away from it. The radiator hose parts arrive today. I will likely assemble that tonight and wait until this weekend to fill and test the system again. I've turned wrenches for many, many years and for whatever reason, this pump vexes me. I won't be a bit surprised if I get it all back together and it leaks from somewhere new. That's about as positive as I'll get for the moment.

      Lines crimped and in place.



      Front and rear of the pump to cover gasket. I'll own this as my own fault. I let it skim and then assembled it all. It would seem that I didn't tighten everything down enough around the ports and caused a poor seal maybe?

      Front
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      Rear
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      And the new hose after cutting and trimming. I'll be putting in a 3" aluminum tube section at the tape mark and shrink sealing it to create my new lower hose. Then it'll be time to fill and leak test it.....again.



      Productive weekend. I got the lower hose assembled and back on the car. Pressure tested everything again and found no coolant leaks. Drove the car a short while to circulate everything and came home. Still no coolant leaks anywhere but I did find oil dripping from 3 of the bolt heads on the driver side of the oil pan. I tightened all of the pan bolts a bit and reinstalled my strut tower brace and hood. Now it's finally time to pull a vacuum on and then fill the AC system.

      Lower hose parts all assembled:


      Getting closer...


      I feel accomplished!


      October 2023:

      I drove my pile down to Casa Grande to a friend's place over the weekend. Why is that a big deal? Because it's roughly a two-hour round trip. And it's hot. I could manage it because 1) I have working AC! and 2) because my pile is trustworthy enough to handle it finally!

      I borrowed some gauges and vacuum pump to pull down the system and check for leaks. When I didn't see any issues, I made plans to charge the system. On a whim, I called a local shop (Charly's Garage) to ask what they'd charge me to fill the system. He said he could knock it out for around $100 and had a spot open that afternoon if I could get it to him quickly enough. I dropped it off at noon and he called me around 3 to pick it up. No issues to speak of and the ac was nice and cold on my drive back to the house in 100* weather.

      I had decided to run some of evaporust's thermocure through the system to get rid of some of the heavy rust inside the block that i found when I had the core plugs out. That stuff stinks when drained. After filling the system with distilled water and adding the rust stuff you're supposed to drive for around 3-4 hours before flushing it out. I drove out to central Phoenix to drop off his pump and gauges and then came back home. After getting back from Casa Grande I had covered enough time to drain and flush the system. Yesterday was spent doing several flushes and refills. I had stocked up on distilled water so I could get all of this done. It's sitting outside right now with coolant in it and everything seems to be good to go.

      While I was at Mike's place, we talked about changes/upgrades to the car. I need to revisit my alignment soon. After having everything pulled apart and stuffed back in, i never went back to check it all. I'm also going to have to sort out the exhaust. I was getting a 90db reading in the car with the windows up and cruising down the highway. That's a bit excessive. I plan to run tailpipes out the back and ditch the side exits. They were never meant to be permanent anyway. I may also switch mufflers. That's all to be decided later.

      Another discussion was wheels and tires. I'm leaning real hard towards picking up the SoT spindles and getting a different wheel/tire combo. I'll contact Street or Track when it gets closer to doing that. Mike tells me that if I decide to run a 275 squared setup, he'll give me more grief to autocross it. And if I run a 295 squared, he'll just take my car and run it himself.

      Anyway, there's the news. I only have a pic or two to share.

      Sitting at Mike's after the drive down. The cooling system burped because I had it overfull a little.



      Here is the first drain of the thermocure stuff....it stinks a bit..ok, A Lot!




      And here are a couple of shots of the Holley tuning software. Hitt and I were looking at why the car wants to stumble when you press in the clutch coming to a stop and what is causing a flat spot around the 2-3k ish range when accelerating 'calmly'.





      Here's the latest. I am generally a patient man. But I hate leaks. And this pile has decided to leak....again.....from the oil pan and water pump. Follow along as I throw money in anger.

      I'm running the ford shorty style water pump:


      It continues to develop a leak between the backing plate and timing cover. This will be the 4th time I've pulled off the pump. I've tried Permatex 22071, Permatex #3, and straight gasket. I've even replaced the timing cover. Each time I've had the pump off, I've run a straight edge over it to be sure nothing is wavy or warped.

      I may be right or wrong, but I feel that the shorty pump has an excellent opportunity to leak from the ports into the timing cover.
      The reason I feel this way is because the standard pump has these two bolts:


      The shorty, does not:


      I called to speak to CVF about their thoughts on this and other things and I have a new shorty pump arriving today along with new hardware. They're also sending me a new crank pulley because I mentioned a constructive criticism of the one in my kit that didn't have an access hole to be able to spin the engine by hand unless the pulley came off. The tech responded with: "Oh, we've since changed that. I'll send you the new style, no charge. Just keep the old one in case you need it for something". They're awesome people. After some discussion back and forth and him stating that they see tons of that pump without issue and I've tried several methods to address it, he would send me a replacement. Again, no charge. His only thought is that the backing plate could be just wavy or bent just enough to allow seeping. So here's the can of worms. What can I do to better my chances of preventing this blasted thing from ever leaking again??? I'm tired of the coolant puddle on my catch pan.

      Along those lines: the oil pan still drools. Not as bad as before but slighty so on the driver's side. When I spoke to Woody at FordStrokers.com, he mentioned that he's not a fan of most modern stamped pans and prefers the Moroso billet end pans. They are pricey....but I happened to find a return on Amazon for $400 off of retail price!!! For that price, I was willing to give it a shot. I could return it if it turned out to be a nightmare. The pan arrived Wednesday. It was unmolested. No hint of gasket material or oil ever touching it. There was a handprint on the base of the pan so I can only assume that a test fit happened and didn't turn out to be what that person needed.





      So that's where I'm at. My weekend will likely consist of putting this pile in the air and draining the oil and water and replacing the pan and pump in the hopes that I can keep the vital fluids IN the car. Along with that, I'm planning on attempting to change the side exits out in favor of tailpipes in the near future. We'll see how that pans out.

      Last pic....I may have over-prepared:


      The replacement pump arrived Friday and is in. I wasn't expecting the blacked out version, though. Doesn't matter to me either way. As long as it doesn't leak. I did a thin layer of RTV on both sides of the pump gasket and the same around the ports on the backing plate gasket. I followed the instructions and let it set for an hour before doing a final tighten on it all. We'll see how it goes.
      I also put a small amount of black RTV around the drooling oil pan bolts. I still plan to replace the pan but I'll wait until it's time to change the oil before I do that.
      I've ordered a few extra bolts that should arrive this week. The socket head screws that come with the front drive kit have taken a beating with all of the remove/install that I've been doing and there were a couple that were feeling a bit sloppy. I'd rather replace those now before getting it all back together only to have them fight me further down the road.

      If this monster stops drooling, the next adventure will be exhaust. I know muffler tone/sound is subjective but I need to make mine more tolerable. I'm considering adding v-bands behind the mufflers when I have the tailpipes added so I can try swapping out mufflers easier. I already have them on the front. I currently have black widows with resonators on it. It was described as 'blappy' with the side exits. I've considered the 50 series flowmaster deltaflow, magnaflows, flowmaster dBX, Borla, etc. I'll have to see which direction this goes.

      It doesn't leak if there's no coolant in it!

      Kris - Building the poor man's '68 Mustang.

    9. #149
      Join Date
      Mar 2022
      Posts
      124
      Wow, great thread. I have similar situations with my car. Always chasing something. Currently it's a rear main seal, which when I purchased the car, the previous owner told me was not a rear main seal, just a oil pan gasket. But I digress...

      Unless I am reading it wrong, it looks like the motor is producing more torque than HP. In that situation, typically it's under cammed. You may know this already, just thought I would mention it. Also the engines never make the power you think they should. I am trying to find out where the 30 to 40 hp is on my motor that I am convinced should be there. The truth is, it probably just isn't there. lol. Love the progress, keep it up.

    10. #150
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      Quote Originally Posted by Pedigry View Post
      Wow, great thread. I have similar situations with my car. Always chasing something. Currently it's a rear main seal, which when I purchased the car, the previous owner told me was not a rear main seal, just a oil pan gasket. But I digress...

      Unless I am reading it wrong, it looks like the motor is producing more torque than HP. In that situation, typically it's under cammed. You may know this already, just thought I would mention it. Also the engines never make the power you think they should. I am trying to find out where the 30 to 40 hp is on my motor that I am convinced should be there. The truth is, it probably just isn't there. lol. Love the progress, keep it up.
      Always something, right??

      And you are correct. It is building more torque than HP. It is a stroked 351 Windsor (408) and all of the early plans where pointing to this being the case. It is a riot to drive. Easily breaks loose on a smooth second gear shift into liberal throttle application. I haven't considered changing anything engine-related though. I won't say that I wouldn't in the future. We can all use that few more HP, right?
      Kris - Building the poor man's '68 Mustang.

    11. #151
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      Got everything reassembled yesterday and took it for a short test drive. No leaking coolant. Met up with Dan and we drove down to our friend Mike's place to talk shop and spend each other's money with future upgrades talk and plan for the SCCA race next weekend. Got home....no coolant leaks. I'll be talking to the exhaust shop this week to see about making some changes soon. I'm just shy of 800 miles on the fresh engine. I think it's almost time to change the oil, swap the pan, and begin the drive-it, flog-it, upgrade-it process!


      Mine is hiding in the shade in the background. Dan is the coyote powered 66 and Mike's is the Chevelle.
      Kris - Building the poor man's '68 Mustang.

    12. #152
      Join Date
      Aug 2012
      Location
      Phoenix
      Posts
      158
      Country Flag: United States
      Not much has been going on lately. I was supposed to go on a vacation to see family during the first week of December but ended up getting Covid from a knucklehead at work that didn't bother to stay home while he was sick. That ate up $600 in non-refundable plane tickets and a week's worth of vacation. Yeah....do the world a favor and stay at home when you're sick....regardless of what you've got.

      I've got a short list (not really that short) of things that I want to address in the near future on the car. But as things go, there is talk of having the roof on the house redone this spring. That could slow progress down a little on the car. I'll have to see much juggling I'll need to do.

      The list:

      Header swap - remove JBAs and add FPAs.
      redo/finish exhaust - add tailpipes at the very least. possibly switch to borla mufflers.
      Swap intake back to Vic jr. from Performer RPM
      Swap moroso billet oil pan on to replace Aviaid stamped pan.
      Swap integrated PS pump reservoir for remote mounted setup.
      Add parking brake setup of some sort.
      sort out fine details in the tune.

      Maybe list:

      swap out valve covers. The fabricated ones aren't bad but they are difficult to work around.
      swap out plug wires. currently running msd sbf universal set and not satisfied with the fitment/clearance.



      ONE MONTH LATER:

      It's been a bit. I've been keeping myself busy doing maintenance on the dailies and relaxing a bit. I have also been gathering funds and parts preparation to begin the list of stuff.


      This weekend I got started on the list.


      I swapped out the Performer RPM intake and went back to the Vic Jr. I'll either need to get a drop base for my air cleaner or trim one of the studs for the hood scoop.



      This is everything just set on top of the intake for test fitting.





      Next up was taking the crossmember off and taking the steering link apart to make getting the oil pan easier to work on.

      A couple of weekends ago I was at a friend's place sorting out the alignment....the one with the chevelle.

      I am holding the wrench on the passenger side and realize he's prepping to tighten the LCA bolt with his 1/2 drive dewalt impact.

      I calmly explain there's no need to go gorilla-mode on it and get a 'got it' in reply......

      I had to order replacement hardware for that side.....

      This was after grinding off the head so I could get the bolt out and crossmember off.





      Anyway....I got the Aviaid pan off and the Moroso on for test fitting. There is so much room now. No clearance issues with the crossmember or steering at all!





      I also ordered a Motorcraft sending unit gasket from amazon. Mine had been drooling a bit and I wanted to get ahead of it getting worse. No pics of that, but I was pleasantly surprised when a pack of 10! gaskets arrived instead of the 1 that I had ordered.....I now have plenty of spares...


      I'm hoping that my FPA headers will arrive soon. This will soon be all buttoned up and then it'll be time to sort out the tune and maybe then I'll have it ready-ish to go fling it around.
      Kris - Building the poor man's '68 Mustang.


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