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    1. #1
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States

      572 cylinder head overheating

      I've got an overheating issue that an IR gun has narrowed down to one particular cylinder. I'm about to tear the top of the engine down for the third time and only have 100 miles on it. Cylinder ...#6... runs 30-40 degrees then comparable cylinder on opposite head
      Setup
      Crate 572 gm
      Manifold single plane modded for fuel injection
      Ron Davis radiator
      Vintage air frontrunner with stewarts water pump

      What I've done to diagnose:
      Had to rebuild engine at first startup due to a metallic object being in #6 and had to replace entire head and piston
      Ran into head heating problem and tore entire engine apart and had block pressure tested and deck cleaned up to insure true surface. Replaced all bearings,crank polished,etc
      Same problem
      Put bypass hose as well as tried without thermostat as per Stewart's advice....no change
      Exhaust gas in antifreeze checked twice...negative
      Plug showing real lean so bumpd fueling up 50% via efi...no change
      Head in affected area gets up to surface temp adjacent to header of 270+
      Intake water temp creeps up to 215-224 without pushing much and temps only drop 2-4 degrees on highway when 75 outside. Placed rubber seal between Rad support and hood
      Sealed Rad to support
      Changed out fuel injector to rule out lean cylinder due to faulty injector...nothing
      driver's head commonly only runs at 205 when good and warmed up prior to entire system overheating
      Thermostat stewarts 180 with bypass holes
      Jacked front of car up to the sky and ran to be sure all air out of system as well as pulled head temp sensor while filling
      Timing initial 17 degrees....advancing of no benefit
      Used factory head gaskets...and only one way to put them on.
      Tried the propane trick to look for vacuum leaks..nadda

      At this point concluding something obstructing head coolant flow....head or block casting
      I'm hoping someone has another idea of what to check before I start the tear down again!
      __________________

      David Beckstrom DVM


    2. #2
      Join Date
      Jun 2010
      Location
      Georgia
      Posts
      2,215
      Country Flag: United States
      sounds like a blockage in the cooling jacket around that cylinder. I had the same problem with one of our shop trucks, and just decided to replace the engine under warranty after a few months of diagnosing / testing things / replacing other parts.

    3. #3
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States
      Not what I want to hear.....no warranty here........backed by bank of me ;)
      Took head off and probed all passages in head and block and all seemed good. Intake water port 30+ smaller than other cool side. Not sure if significant but physically would flow about half of cooler side.
      David Beckstrom DVM

    4. #4
      Join Date
      Dec 2010
      Location
      Fredericksburg, VA.
      Posts
      3,155
      Country Flag: United States
      My first thought is, are you sure the pistion matches the others? Have you run a compression test on the engine to see if the compression in that cylinder is the same as or close to the others? I'm thinking that perhaps that cylinder is running at an elevated compression relative to the others causing excess heat.
      Steve Hayes
      "Dust Off"
      68 Camaro

      Given sufficient initial acceleration, even pigs can fly!

    5. #5
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States
      Compression of that cylinder almost exactly the same as the adjacent ones.
      David Beckstrom DVM

    6. #6
      Join Date
      Sep 2006
      Location
      Henderson,NV
      Posts
      2,870
      Country Flag: United States
      When you increased the fuel to that injector, did the plug fatten up?
      Todd

    7. #7
      Join Date
      Nov 2006
      Location
      Houma, Louisiana
      Posts
      305
      Country Flag: United States
      Is it possible that you have the wrong rotation Stewarts water pump? I also have a 572 with zero cooling problems, I have a Griffin radiator with double row of one inch tubes being cooled by twin 12" fans, this keeps the 572 cool with no problem. It rarely sees 205 and then only in traffic.. On the road it runs 180-185.


      Bill Haynie

      1970 Nova 572/620 TKO600
      2013 Boss 302 Laguna Seca



    8. #8
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States
      I took the water pump off and opened it up and sent pics to Stewarts and they confirmed it was correct for reverse rotation vintage air. I was sure hoping that was it.
      Re Fuel injector....when I enriched it 50% I didn't drive more than a mile or so and didn't notice much color change but didn't expect with that short run. I just know the head temps didn't do a thing.
      Took head and intake as well as pics to engine/machine shop. They are scratching their head also. That chamber looked leaner than the other rich ones but not like it was super lean or anything. Exhaust valve was brownish vs black on all the others. They really don't think the Lean thing is the original cause of heat production.
      So, thats all the good new and bad news...nothing definitive. Someone suggested swapping the heads and see if the heat follows . If it weren't such a big pain in the butt I'd likely try that. On drivers side to get to lower head bolts with header in there I've have to disconnect hyraboost, clutch linkage, etc and that may still not be enough. The side I'm doing is barely able to get those bolts and got little in the way...except those headers. I too sick of chasing this to pull the motor again (3rd time in 5 months) to swap heads....lol....plus I don't think thats it anyway.
      David Beckstrom DVM

    9. #9
      Join Date
      Nov 2006
      Location
      Houma, Louisiana
      Posts
      305
      Country Flag: United States
      You have a pm


      Bill Haynie

      1970 Nova 572/620 TKO600
      2013 Boss 302 Laguna Seca



    10. #10
      Join Date
      Sep 2006
      Location
      Henderson,NV
      Posts
      2,870
      Country Flag: United States
      My thought was the computer is not increasing the pulse width on that cylinder correctly. Check the terminals in the connector for that injector as well. You should also see your oxegyn sensor go rich by fattening up that cylinder.
      Todd

    11. #11
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States
      Todd I'm definitely going to chase down the electronics of that injector today when I get it all back together. What I've done so far is rule out the block for any coolant blockage and pretty much the head also. I ported out the water outlet on the head just in case. I never thought I'd ever be porting something like that but at this point without anything else jumping out to explain want to take that off the list of possibilities.... I moved the bypass outlet to the middle position on the intake rather than the heater outlet . I noticed that when the engine was hot the bypass hose was pumping( sucking actually) 215 degree water from that hot side of intake back into lower hose and really heating up that hose(195-200) which meant water pump was then pumping 200 degree water back into the block. Again I don't know if that will make much difference but trying to tweak anything to help me out.
      Attached Images Attached Images        
      David Beckstrom DVM

    12. #12
      Join Date
      Sep 2006
      Location
      Henderson,NV
      Posts
      2,870
      Country Flag: United States
      The only time your bypass hose should be an issue is when the thermostat is closed. It was designed to allow coolant to recirculate through the block and prevent cavitation and an air pocket until the t stat opened.

      It looks like your intake gasket slipped and was much to low last time around. OR, you have the wrong intake gasket/intake needs planed down to lower it. Look at the seal in your photos. Its low on your water outlet and air intake. I think a vacuum leak was a real possibility even though you couldn't nail it down.
      Todd

    13. #13
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States
      The gasket was fairly centered on the holes but the floor of the intake water port was that much higher than the head floor...one more reason to open it up. On the intake air port it was maybe 1/8 " low is all. I'll try to make sure it is up better when I mount this time. When mounting the intake it can be centered vertically when setting in but once the bolts start to pull it down gasket wants to go with it.
      David Beckstrom DVM

    14. #14
      Join Date
      Sep 2006
      Location
      Henderson,NV
      Posts
      2,870
      Country Flag: United States
      Look at your upper right hand photo. Looks like a good .25. You have a **** hair of seal on the water port in that photo and I can't see the top of the air port but it looks super low. Make sure you are getting the intake on nice and square before you tighten down the bolts as well. Don't discount a mis machined intake. I learned that lesson the hard way a long time ago.
      Todd

    15. #15
      Join Date
      Nov 2006
      Posts
      152
      Country Flag: United States
      I would swap injectors and see if it follows, also check wiring and injector driver

    16. #16
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States
      Already swapped inj..no change. After previous changes seems to be less discrepancy of temp but still gets overall hot. Today was 9 and overall got up to 222 and highway driving a couple miles made 0-2 degrees temp drop. Upon stop and go as well as idling no temp drop at all. So shut er down. I noticed at idle once hot it gun showed 225 at upper hose near intake yet near radiator was 208 as was lower hose. Makes me think reduced flow through radiator....but then why wouldn't Rad temps get even lower with fans blowing lots of hot air?
      David Beckstrom DVM

    17. #17
      Join Date
      Sep 2006
      Location
      Henderson,NV
      Posts
      2,870
      Country Flag: United States
      Have you made sure the t stat is opening at the proper temp and fully? Boil it or replace it. Also, pull the cap once the stat opens and watch the coolant flow. It should really be moving. Your upper to lower hose temp drop is suspect. It should be better than that. I'd say at least double. Big inch big blocks don't cool that great around town even with dual spals unless you have larger than 13" fans and an oversize radiator. However, my 489 ZL1 will run under 180 all day long on the highway even up to 100 degrees ambient. You have a cooling problem of some sort. I'd start with the basics.
      Todd

    18. #18
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States
      Yep it was basic but not apparent. I finally decided to pull the radiator even though it looked good inside. Filled with dishwashing detergent solution a nd soaked an hour flushed and got lots of weird brown stuff out. Soaked with a triple shot of prestone cleaner, soaked and flushed and looked inside to lots of brown slime. My guess is previous owner ran dex cool. I fabbed up a way to flush each individual tube with water pressure. Worked like a charm and temps stay around 184 now.
      I would have had done professionally but under the gun to get to transporter for power tour in 2 days.
      I think the cylinder was one that runs warmer anyway and just exposed the cooling deficit.
      David Beckstrom DVM

    19. #19
      Join Date
      Sep 2006
      Location
      Henderson,NV
      Posts
      2,870
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      The lack of cooling across the core was the key. Glad you found it.
      Todd

    20. #20
      Join Date
      Sep 2007
      Location
      Denver
      Posts
      325
      Country Flag: United States
      OK, too optomistic too soon. Was 80 here yesterday so thought I'd test her out. Was great for 20 min. then just continued to climb. Ultimately was up to 212 idling in driveway not really cooling down much at all. Suspecting Rad gumming up again. Will pull it out and have professionally cleaned and hopefully flow tested. Power tour option mostly out now. Big bummer.
      David Beckstrom DVM

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